PT Indonesia TRC Industry is a manufacturing company that produces components
made from rubber, metal, and plastic. One of the quality problems in the Roll Press
Department is the high number of not good (NG) products in the rubber press
process. Based on February 2026 data, the NG percentage in the Roll Press
Department reached 9.02%, while the company target was 3.17%. Priority analysis
showed that the Roller Paper Eject part contributed the highest number of NG
products, with outer tear as the dominant defect. Under the existing condition, this
part produced 809 NG pieces out of 8,400 actual production pieces per shift, or
9.63%. This study aims to design a process improvement proposal for the rubber
press process to reduce NG products with outer tear defects on the Roller Paper
Eject part.
The problem-solving process was carried out using the DMAIC approach through
the Define, Measure, Analyze, Improve, and Control stages. The Define stage was
used to define the problem, scope, target, primary metric, and project focus through
a project charter. The Measure stage collected data on machine start interval, panel
temperature, mold temperature, and the number of NG products as the response.
The Analyze stage was conducted using a fishbone diagram, Five Whys, and Design
of Experiment (DOE). The Improve stage was carried out through Response
Optimization as a further analysis within DOE to determine the parameter
combination that minimizes the number of NG products. The Control stage was
conducted by preparing process control recommendations in the form of a proposed
work instruction draft.
The results showed that the main improvement parameters were machine start
interval and mold temperature. Based on the Response Optimization results, the
optimal combination was a machine start interval of 186 seconds and a mold
temperature of 162.655°C. This combination produced a predicted NG value of
1.35472 pieces out of 200 pieces, resulting in an optimized NG percentage of
0.68%. This indicates a potential NG reduction from the existing condition of 9.63%
to 0.68%. The proposed improvements include setting the machine start interval,
controlling mold temperature, adjusting panel and mold temperature, and
preparing a proposed work instruction draft. The financial impact analysis showed
that the proposal is potentially feasible, with an initial investment of Rp12,766,800,
an NPV of Rp5,345,871, a monthly IRR of 6.36%, a BCR of 1.42, and a payback
period of 9 months.
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